Quinton Gas Rig Explosion: Animated Timeline Released By Safety Agency

Thursday, August 16th 2018, 12:46 pm
By: News On 6

A safety agency just released an update on its investigation into the explosion at a Quinton gas rig that killed five men on January 22, 2018.

Matt Smith, 29, of McAlester; Parker Waldridge, 60, of Crescent; Roger Cunningham, 55, of Seminole; Cody Risk, 26, of Wellington, Colorado and Josh Ray, 35, of Fort Worth lost their lives in the explosion. Survivors of the men have filed lawsuits against rig operator, Red Mountain Energy and the drilling contractor, Patterson-UTI.

On Thursday, the U.S. Chemical Safety Board released written and animated timelines of the actions that led to the explosion. Crews were in the process of changing out a drill bit which involved removing a drill pipe from the gas well.

8/1/2018 Related Story: OSHA Issues Citation To Companies Connected To Deadly Quinton Rig Explosion

In that process, investigators believe gas entered into the well during the operation which is known as "tripping." Mud and gas blew up from the well and ignited, causing the large fire.

Here is the timeline released by CSB:

  • January 21, 2018: Crew members from the Patterson-UTI Drilling Company had been drilling a gas well for over a week. Activities were being overseen by the operator of the well, Red Mountain Operating, LLC (or RMO) in Pittsburg County, Oklahoma. 
  • At 3:36 pm, the Patterson crew stopped drilling to remove the drill pipe from the well and change the drill bit.  
  • At 6:48 pm, crew members began the process of removing the drill pipe from the well. The Patterson crew pumped mud into the well during the removal of the drill pipe with the intent to keep the well full of mud. That operation involved closing an isolation valve to prevent mud from flowing out of the well.  By 10:30 pm, the end of the drill pipe reached the top of the curve in the well. 
  • January 22, 2018: At 12:35 am, the crew pumped fluid also referred to as a “weighted pill” above the top of the curve to prevent gas influx into the lateral portion of the well. 
  • At 1:12 am, the crew began removing the drill pipe from the vertical section of the well. For this portion of the operation, the Patterson crew performed a “Continuous Fill” tripping method. Mud was continuously circulated in the wellbore using the Trip Tank pumps to keep the well full by replacing (?) the volume of the drill pipe removed with drilling mud. The isolation valve was open for this operation. 
  • At the start of this procedure, the drill pipe started pulling ‘wet’ – meaning the drill pipe being removed had not drained and still contained mud. The Patterson crew was aware that the pipe was plugged. At this point the Patterson crew attempted to pump a volume of mud also referred as a “slug” into the drill pipe to push the mud that remained in the drill pipe out, but this was not successful as the drill pipe was plugged. Therefore, the drill pipe in the vertical section was removed while it still contained mud. 
  • By 6:10 am, the drill pipe and drill bit were completely removed from the well. At that time, the driller closed the blind rams on the well’s blowout preventer. 
  • At 7:57 am, the driller opened the blowout preventer blind rams so that a new piece of drilling equipment called a bottom hole assembly could be lowered into the well. At 8:09 am, mud was pumped through the bottom hole assembly to test the new equipment. 
  • While the rig crew tested the bottom hole assembly equipment, the mud pits gained 107 barrels of mud. Mud pit gains are an indication of a possible gas influx in the well. Data obtained by the CSB indicates that conditions existed that could have allowed a gas influx into the wellbore during the tripping operation. 
  • At 8:35 am, with testing complete, the bottom hole assembly was lifted out of the wellbore. At 8:36 am, mud blew upwards out of the well. The mud and gas from the well subsequently ignited causing a large fire.